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[A380] 空客关于飞机在滑行阶段出现Landing MEMO信息的解释。

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四川航空

发表于 2011-5-22 23:21:00 | 显示全部楼层 |阅读模式 来自: 中国四川成都

Flight Warning Computer (FWC) – LDG INHIBIT memo displayed on ground before T.O.

 

ATA                      3153

AC Type                A318,A319,A320,A321

 

Description

Operators might report that A/C experienced display of LDG INHIBIT magenta memo on ECAM on ground before T.O. As per FCOM 1.31.15 , it should come up in FP 7 and 8 . What are Airbus advice regarding this memo occurrence?

 

Reference

 

SIL 34-084-ERRATIC AIRSPEED INDICATION – PITOT PROBES MAINTENANCE ACTION

 

Solution

 

According to ESLD FWC standard page 2.0.320 , this office confirms that LDG INHIBIT memo is displayed either into flight phase 7 or 8 when there is no flight phase inhibition overridden. Furthermore, we remind the airline that on ground the aircraft is into flight phase 2 when there is at least one engine running (not in T/O power) and aircraft speed is below 80 kts.

 

Please find hereafter a sum up of flight phase 7 and 8 triggering conditions:

 

-          Flight phase 7 is triggered while the aircraft is not on ground but below 800 ft, provide that both radio altimeters are operating and no immediate ground detected.

-          Flight phase 8 is triggered when aircraft is on ground, engine 1 or 2 running (not in T/O power) and aircraft speed below than 80 kts .

 

Airbus assumes that a wrong FWC flight phase computation could have led to the display of LDG INHIBIT memo. Indeed, it might be possible that FWC has computed spuriously flight phase 7 or 8 due to an erroneous data. Airbus would like to inform the airline that some operators have already reported such misbehavior in the past.

 

1/ it could happen that humidity, reflection or radio altimeters fluctuation disrupts data acquiring. Then if the altitude computed and provided to the FWC is not equal to a ground value, flight phase 7 will be unduly triggered instead of flight phase 2. In that case, it will be possible to generate the LDG INHIBIT memo. Generally, water located into the antenna is the root cause of these disruptions related to radio altimeters. Therefore, we recommend the airline to verify that there is no humidity trace infiltrated into RA antennas in case of reoccurrence.

 

2/ furthermore, FWC may confuse flight phase 2 and 8 whether the Boolean speed value is corrupted. Therefore, the FWC will generate a flight phase 8 instead of 2, enabling the triggering of the LDG INHIBIT memo. The assumption that could explained an airspeed up to 80 kts, while A/C stopped on ground, is a pressure trapped in the tube by water ingress. Moreover, on ground when the aircraft is stopped the computed airspeed is set to “No Computed Data” as long as the speed is lower than 30 kts. If an airspeed up to 80 kts was experienced during the event, this airspeed should have been observed on PFD Capt and F/O.

 

Regarding the airspeed generated by ADR 3 (not displayed), only an existing airspeed on dedicated stand-by instrument could have been noticed. In case of reoccurrence, Airbus recommends to perform the following AMM Tasks as a trouble shooting procedure (note that airline can also refer to SIL 34-084):

 

-          34-11-15-200-001 Inspection/Check of the Pitot Probe (9DA1, 9DA2, 9DA3)

-          34-10-00-170-001 Flushing of the Principal Total Pressure Lines

-          34-10-00-170-003 Draining and Flushing of Standby Pneumatic Circuits

 

心如磐石,形如水~!!!
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发表于 2011-5-22 23:33:43 | 显示全部楼层 来自: 中国福建厦门
不明白  高手解释一下
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实名认证昆明隆瑞

发表于 2011-5-23 07:12:29 | 显示全部楼层 来自: 中国云南大理白族自治州

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嘿嘿!谢谢分享
男人是来征服世界的
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发表于 2011-5-24 20:57:00 | 显示全部楼层 来自: 中国四川德阳
看不懂的鸭梨大啊。。
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实名认证

发表于 2014-5-27 21:04:44 | 显示全部楼层 来自: 中国广东
不明白。。。。。
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发表于 2014-5-28 11:29:40 | 显示全部楼层 来自: 中国四川成都
意思就是这种情况可能是假信息。
检查当时地面是否有反射物影响RA,或者信标收到信号混淆了飞行阶段,或者FWC产生虚假信息。
大概就这意思,没逐字逐句的读。
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实名认证

发表于 2014-5-29 21:16:58 | 显示全部楼层 来自: 中国浙江杭州
唉!英语没学好啊
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